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CJN8

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Everything posted by CJN8

  1. Distributor checks out and is set to spec. Also, the leak down test percentages evened out after the engine was warm, averages were about 9% to 11% which is pretty good I guess. I emailed Hesco and they said put 1/2" spacers under the CPS bracket and re-adjust my CPS to proper clearance. I did that today and it adjusted my base timing from 14* BTDC to 7* BTDC. I took it for a spin and no sign of any issues. My manifold vacuum went from about 17.5 to 16.0. I suspect this timing adjustment should make a difference in NOX production, only one way to find out. I will report back. Thanks Moses!
  2. So my detective work continues. Have you heard of setting fuel sync on the mpi kits and the jeep 4.0? The distributor does not adjust timing but I guess it does adjust fuel synchronization? Could this be an issue?
  3. Preliminary test while motor was not warmed up. I wanted to get my technique for finding TDC down. I used a vacuum/fuel pressure gauge so I could see exactly when the piston was at TDC. Worked like a charm Front of motor 1. 15.6 PSI (intake/exhaust manifold no hissing noise, valve cover hissing noise) 2. 12.2 PSI (intake/exhaust manifold no hissing noise, valve cover hissing noise) 3. 8.8 PSI (intake/exhaust manifold no hissing noise, valve cover hissing noise) 4. 7.7 PSI (intake/exhaust manifold no hissing noise, valve cover hissing noise) 5. 8.8 PSI (intake/exhaust manifold no hissing noise, valve cover hissing noise) 6 11.4 PSI (intake/exhaust manifold no hissing noise, valve cover hissing noise) Back of motor I am going to warm the motor to operating temp and repeat the test. Nate
  4. A little more diagnostics...I looked into the catch can which is between the valve cover and the intake manifold. The crankcase gases appear to have both oil and water present, probably due to the short trips I have been taking. I looked at the engine oil in the crankcase and there is no water or coolant there. I also looked at the coolant and there is no oil. I ordered a leak down tester today. The unit is made by OTC and got good reviews on amazon. I hope the test is telling. I will report back. Thanks for all the help Moses, it is much appreciated.
  5. From your write up on the FJ40... This engine ran sluggishly, the result of inadequate cylinder seal at the rings. The valves seated, the head casting and head gasket were fine, however, the combustion gases leaked past the rings and into the crankcase. Engines like this have a distinct "blow-by" smell in the crankcase oil. While the PCV system can recycle blow-by gases, the remnant of combustion gases remains in the oil. I have often referred to this odor, notable with the oil filler cap removed and the engine running, as the "smell of death" Bingo...this is how my oil smells, even after a change and I drive for 20 miles its there. I ordered a used oil analysis test bottle from blackstone labs on Monday to test this smell. I need to find a leakdown tester. Great help Moses. Thanks so much.
  6. The compression numbers offered earlier were before the rebuild. When I tested after the head rebuild I got about 135psi even across all cylinders. The shop doing the testing say it is 171, 174, 175, 174, 174, 170. I plan to test it again this weekend to verify the numbers. I am using a cheap harbor freight compression tester, maybe mine is not accurate? The real interesting thing is that I am really not getting any spark knock. I drove it home from the smog repair shop yesterday and pulled a long grade in 4th going 65mph and had no real issues with pinging. I do run 91 octane. I have the 4.2 cylinder head still. Yes I removed all spark plugs and held down the throttle during the compression test. I plan to re do the test this weekend to check my old numbers (maybe my HF tester is not as good as the shop tester). Could a small casting flashing bump cause the high NOX? I have been going through my head and I seem to remember that there was a small bump on one of the cylinders near one of the valves.
  7. I just recently had the head reconditioned. However, the Jeep failed NOX, roughly with the same numbers before the head was reconditioned too. The pistons were cleaned prior to the install of the reconditioned head. I have spent thousands trying to get my Jeep back on the road...my options have run out. My base timing is 14 BTDC, when I put spacers in will I see the timing drop? Will this be visible with a timing light?
  8. How do you space the pickup on the front of the motor down? How much spacing? Do the spacers go between the aluminum bracket and the oil pan? Regarding the head gasket I used a run of the mill felpro. Is their a better choice that is thicker?
  9. It has been a while since i updated the status of my NOX issue. I finally broke down and took the Jeep to a reputable emission repair facility. They smoke tested the exhaust system and found that the header collector before the catalytic converter was leaking so they replaced the flange before the catalytic converter as well as the one directly after the catalytic converter. They were able to pass the low speed test but it still failed the high speed test. They continued working through the issue by testing the fuel trims, smoke testing the intake, looking at timing, etc. etc. In the end after ruling out all other potential issues they performed a compression test and noted that all six cylinders were in the 170 to 172 psi range. They said, which I verified, that factory compression numbers should be between 120-150 psi. In the end the diagnosis was that the higher compression is creating more NOX which is no being sufficiently scrubbed by the aftermarket magnaflow catalytic converter. They recommended either the factory 1995 4.0 catalytic converter or a larger catalytic converter with the appropriate EO number. The saga continues...can you even get a factory converter anymore
  10. 14 degrees base timing, it hunts a little but that is where the timing mark holds the majority of the time. The slop in the timing chain is about 3 degrees when I rotate to TDC then rotate back until I feel the slack in the chain take up.
  11. Thanks for all the help Moses. I ran a manifold vacuum test and am getting 16" with a steady needle. Seems this is pointing to a timing issue? I have not run a leak down test yet but it is in my plans. The MAP test was performed using a hand vacuum pump and digital multimeter. Could a lean running MAP effect manifold vacuum? I have read that lean conditions and low normal manifold vacuum go hand in hand, true? Thanks again, Nate
  12. Tested the MAP sensor today. Does this explain my lean condition?? My Readings: 0" vacuum = 4.77 v (1.5% greater than below) 5" vacuum = 3.23 v (17.2% less than below) 10" vacuum = 2.38 v (20.6% less than below) 20" vacuum = .75 v (31.8% less than below) Diagnostic info from an article in Four Wheeler Magazine: 0" vacuum output should be 4.7 volts. 5" vacuum output should be 3.9 volts 10" vacuum output should be 3.0 volts 20" vacuum output should be 1.1 volts More voltage equals a richer condition, less is leaner. Even a small variance (0.2 volts) can make a big difference in air/fuel ratio and drivability. http://www.fourwheeler.com/how-to/engine/1401-driveway-diagnostics-map-sensor/
  13. Radiator fixed! I had it cleaned, pressure tested, and leaks soldered. I went for a test yesterday and I continue to fail high speed NOX, roughly about 1400 PPM with a max passing value of 1066 PPM (~30% over passing value). I am very happy with how the motor runs after freshening it up. Other than the valve cover splash guards that I installed I have no other baffles, I am getting zero oil in my clear catch can. After I put the splash guards in I put red loctite on the nuts, I decided to JB weld the nut for added safety. In hindsight I should have pulled out my MIG welder and put a few small tacks on the nuts. I can rule out?: - Carbon deposits, head is new and piston tops were cleaned - Cooling system, radiator cleaned and serviced, new water pump, new 195 degree thermostat, new hoses, new coolant (runs in the middle to middle lower green range on the gauge) - Fuel pressure, 34 psi at key on, 30 psi at idle, 40 psi when i remove the vacuum line Possible lean condition? - Injectors? - Map Sensor? - Higher fuel pressure? - O2? (I replaced it in 2009 but did not use a mopar factory sensor, heard that some O2 sensors do not switch fast enough to control lean conditions) - Catalytic converter? (has a carsound unit that I purchased in late 2008, this was before you had to have a CARB stamped converter, maybe not strong enough to handle NOX?, this converter has never really produced good NOX numbers) - ?? I know that the jeep is able to produce low NOX readings, in 2004 it blew 46 PPM at 15 MPH and 28 PPM at 25 MPH with 35" tires on.
  14. The reason i had excessive carbon buildup was due to the baffle design of the Westside Performance valve cover. The baffle was essentially a cup with small slits in the bottom. Not good, the oil would collect in the cup and when it got substantial enough the CCV would take a big gulp and that was that. All that oil would run through the motor = carbon buildup. I verified this buy running it with an inline air/oil separator. This is how I corrected it. Removed the original baffle Made a proper baffle Made a valve cover crossover tube to move the CCV further from the original location The Cat I am running has the air injector tube capped. I have fired the motor and it runs great, even took it for a test drive and no major issues. The only issue is the radiator is now leaking around where the filler neck is soldered on. I was thinking I could just have it re-soldered but maybe it would be best to replace this 33 year old radiator. The fins are a mess and it looks like one of the tubes was fixed in the past. Any recommendation regarding where to order a new radiator? I am partial to the brass/copper HD OEM rads.
  15. Status update. I removed the head and as thought had a considerable buildup of carbon across all the cylinders. I had the head fully reconditioned, reworked the baffles on my valve over, installed new thermostat, fully cleaned the intake manifold that was coated in motor oil. Surprisingly the cylinders looked to be in good shape, some cross hatch visable with no ridge. The motor had .060 Pistons installed so for sure this motor was rebuilt. One of the last items replaced was the water pump. The strange thing was it had a reverse rotation pump installed on a V belt motor?? I replaced with a standard rotation pump. I have not fired the motor, plan to do that this weekend. Any words of wisdom to provide prior to firing either the new head?
  16. Thanks for the reply. Yes, there is evidence of oil entering the combustion chamber through the CCV (which is in line with cylinder 4). This is why I built a crossover breather tube for the valve cover. The CCV was too close to the baffle in the valve cover and it would pull oil into the manifold when I drove down hill and rolled off the throttle. I verified this by putting a air/oil separator in the rear CCV to manifold vacuum line. Lee over at hesco recommend building the crossover tube so I did. How do I check the manifold vacuum and base timing degrees? Thanks! Nate
  17. Thanks for taking the time to read my post and offering up some good food for thought. I guess my next question is what is the factory spec for compression on the 258? I have read 120-150 does this sound correct?
  18. Vehicle background: 1983 Jeep CJ7 Laredo 4.2 with Hesco MPI kit Westside Performance Valve Cover (thick cast aluminum replica of the stock cover) T-18 four speed Dana 300 Dana 44 axles front and rear (4.27 to 1) 36" Swamper TSLs I bought this Jeep in 2003 odometer had 145,000 miles, now has 170,000, it does not get driven all that often. Plaque on the motor reads "MOPAR Performance", it is a mopar 4.2 crate motor with a remanufacture date of 1998. My estimate is that the motor has ~80,000 miles on it. Issue: Recently failed low speed NOX during my last CA smog test, measured 1,322 and max is 1,066 (fail). High speed NOX readings were measured at 948 and max is 968 (pass). For the last 3 or 4 tests high NOX have been an issue. Before I went to test my jeep I changed the oil, it was a quart low. I removed and cleaned the plugs. The fourth plug from the front had quite a bit of carbon buildup. After the test i decided to do a compression test. Got the Jeep up to operating temp and did my first test dry. Readings from front of motor (water pump) to back were 121, 128, 123, 137, 124, 122. The fourth cylinder had a compression reading about 10% greater than the others. This was the same cylinder that the spark plug with the carbon buildup came from. Next I performed the same test but this time adding two squirts of oil to each cylinder before the compression test. My readings were within 1-2 psi of my dry test. My diagnosis is that the cylinder head needs to be rebuilt. The cylinder head is worn letting excessive blow by enter the combustion chamber through the CCV valve which vents to the number 4 cylinder where the oil is burned. This is why i was a quart low when I changed the oil and why cylinder 4's spark plug was all coked up. Does this sound reasonable? Can i rule out rings in this case? What do you think? Thanks for the help!!
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