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Nucking Futs

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Everything posted by Nucking Futs

  1. Thanks Moses. I have Howells TBI kit, and I do not have emission requirements on my Frankenstein Jeep. The engine is an 84 so that is how I define my Jeep since this is the heart of the performance. While I cannot say money is no object, I can afford either a stock rebuild, or a 4.6L stroker or V8 swap. I am cognitive of cost and exercise discretion when it comes making these kind of changes. I will ask a lot of questions, ponder for weeks, and act slowly on my decision. It took me a year before I removed the T5 and installed a Ford NP435 (feels at home in the Jeep). My baseline data is the 4.2L. I started with a stock 4.2L with the BBD feedback carb, did the Nutter Bypass with Ford big-cap rotor, added MSD CDI, then the TBI. All changes made improvement in drive ability and reliability. The TBI was by far the best improvement. Not necessarily performance increase in HP and torque (some though), but rather made her very reliable and drivable. Highway speeds have been my problem, and as you noted with the 4.2L head issues, is exactly what I experienced driving on the mountain roads. I know the 4.2L can do better, as I have to back off the throttle because of pinging. With this knowledge, I think you answered an obvious question that I failed to see. The head will contribute more towards drivability. This is a performance increase in itself and will be worth the expense alone. So, if I keep the 4.2L, she will at least be getting a 4.0L head. I better start looking at short tube headers now too. But a 4.6L stroker with an increase in bore diameter. Hmmmm...............Haha, there is no replacement for displacement! Which makes me chase the V8 swap idea too. Thank you again sir.
  2. The 4.2L is done. Blow-by in crankcase is so excessive now, the increased pressure cannot be managed any longer. Time to pull her out for some major surgery. I am considering the 4.0l head swap, but I am not certain that the extra cost to swap the head is going to help that much to justify the cost. I understand the 4.0L head flows better than the 4.2L head, and is overall a better design. I would like a little more top end power without losing the low end grunt. But.....when I see HP and torque numbers on 4.6L strokers (or a 4.2L with 4.0L head), it is always around 2500/3000-5000 rpm. This is way outside what I care about. I would love to see what the power band will be from idle to 3000 rpm with the 4.0L head on a 4.2L (or a 4.6L stroker). I am not looking for a power monster, just a little boost. I would hate to spend money on a new head, exhaust manifold, and exhaust system, only to find out that it really did not add performance increase where I want it. Does anyone have some useful information they can share? Real data would be optimal, but anything would help. Will the head swap help below 2500 rpm to warrant the cost?
  3. Thanks Moses. My next journey is to find a quality builder. I do want to have the engine balanced. From my understanding, it will smooth out the engine more which will also aid in prolonging the overall life of the engine, a worthy investment of cost. Searching the internet I have found several business that offer new casting 4.0L heads, and others that prep the head for the 4.2L. Hesco still makes their 4.0L head, and there is always Edelbrock's head. The later two are expensive, and I don't want to blow half the budget on just the heads. I will be visiting the local auto recycler yards in search of intake and exhaust manifolds. I will need to contact Howell about the O2 sensor locations between the 4.2L and the 4.0L stock locations. I don't think it will make a significant difference, but I am sure they will know. I do have a question about cams. I know you previously were a proponent for the Comp 264H grind (I believe that was the one) from one of you videos you made. Considering that I have the Howell TBI and the associated MAP sensor, what differences in cam profile are needed for the TBI system? I drive and live in the low to mid power band, I generally keep the engine under 2500 rpm. That is the sweet spot of the 4.2L. More to come and I will post progress as it happens. One good outcome from all this is I will have a fresh new rebuilt engine.
  4. Hi Moses. I think the wind was sucked out of my sail after my last go around with the Jeep. Not as good of news as I was hoping, but could be worse. The engine still runs at least. Here is the report. With the valve cover off, I visually looked to see TDC for #1 and went around several times and tested at both positions just to make sure. I did observe the rotor for a last double check. I watched for the rockers to stop moving, and wiggled them to see if there was any tension on them. No tension present with just a slight twisting from my hand on the rockers at TDC. Looking at the timing mark at TDC, it appears that the valves are closed when they are suppose to be. When I did the leakdown test, the engine did not spin, another indication I was at TDC (if I am not at TDC the engine will spin forwards or backwards as I apply 100psi). Sigh! I still have ~45% leakdown. This is disappointing. I was hoping for a simple timing set replacement. Kind of weird that compression numbers where so high with that much leakage. I would say one of the gauges is wrong. Since I can hear air escaping into the intake manifold, I would bet the HF compression gauge is likely off. I need a new timing sprocket/chain this I know. I also have an internal vacuum leak via the intake valves, this I know. The leak could explain why it wants to idle a little higher. The spark knock I would say is from the excess carbon. I thinking that my cylinder head needs servicing, more than I can do. Either carbon is hold valves open or the issues with stem and/or seats, and likely a combination of all of these. If my cylinder head does need work, doing just a top-end rebuild doesn't make sense with 170,xxx miles. I was always taught this with speed accelerate wear on the piston rings. I have some thinking to do. In the meantime, I would like to hear your analysis Moses.
  5. Moses, at this point I would say anything is possible! What I do know. I have an C-block with serpentine belt drive. The timing cover has the magnetic probe socket. Is the V-belt cover compatible with the serpentine belt? Pulling the valve cover may be best option at this point since the possibility of mismatch parts is plausible. While I don't think this has happened, I need to verify this to rule out uncertainty. I employed the visual method of looking through the spark plug hole to find TDC. I know that there is a moment when the up-travel stops and the crank is still spinning . How many degrees am I off from true TDC I don't know, but I am close enough that the valve is suppose to be closed at this moment. Looking at the timing mark it is around 4* before and valve is open. If I rotate the crank to the TDC, valve still open. Past TDC and the air pressure will push the piston down. If I try 8* before, the air pressure will spin the crank backwards. Because I am looking at TDC for timing and not the timing mark, this is why I am thinking there is cam timing error. The stretch in the chain has me thinking the chain jump may be a real possibility. So I will pull the cover off and verify when the valves are closed according to the rocker arms. I can then see where the timing mark is. If you know approximately how far off the IH cover is from the Jeep cover that would be helpful. For creep, I'm probably on my own. Inspection of damper when timing gear and chain is replaced may tell. And the Jeep passes smog with no issues btw. The tool looks like a winner and will add it to my collection. In the meantime I have some work to do.
  6. Quick lunch break test. Timing mark set at TDC. #1 cylinder visible through spark plug hole. Rotor pointing towards #1 position on cap. #1 has 45% leakdown with air moving through intake (sound adjustable by opening butterfly in TBI). Without rotating engine, I removed the hose and tried #6 to see if I was on wrong cylinder. #6 had leaked also. I tried various positions on the timing mark to see if I could find where valve was actually closing. I could no find it as psi pushed piston either backwards or forwards depending on position in stroke. I tried putting a wrench on the crank nut to lock crackshaft from moving, but I had moderate success doing that and still had leakage. I need an extra set of hands! The only way to positively know when valves are closed will be to remove the valve cover off. I may do that later. I decided I would try something a little easier and see how much stretch is in the timing chain. I rotated the engine all the way around to take up slack and I set timing make to TDC on timing cover. I then rotated the crank back until the rotor moved. It took between 3/4rd" to 7/8th" of an inch of movement on the dampener before the rotor moved. That is past the 5/8th" you mentioned. Considering the slack in the chain and my valve closings do not seem to match TDC I am still thinking: (a)-the chain is unable to keep time because of the slack, or, (b) chain jumped and is out of time. I can verify #1 intake valve closing and opening by pulling off the valve cover, rotor through the cycle, and note the position of the crank timing mark in relation to the #1 intake valves opening/closing. But is that really necessary and worth my time with that much slack in the timing chain? I think doing anything else it is an exercise of futility. As you stated, compression numbers are good. Even if the numbers are off 20%, they are still good. I know I need a new chain. In a real simplified way, I see the compression test indicates that my engine is holding air just fine. The leakdown test says I have a timing issue in relation to the movement of air at the correct time. I don't know 100% though. I'm not a mechanic, I just play one on the internet :D.
  7. Moses, I'm pretty sure I did it correctly. If the timing mark is on TDC, #1 is up to top, the rotor is pointing to #1 plug wire, I should be on intake stoke, yes?. #1-6 are paired but #6 at exhaust and #1 at intake I understand. #2-5, #3-4 are paired if I recall correctly in the same manor. I did follow the firing order, noted where the rotor is in relation to the cap for firing and position of cylinder. I can redo the test to verify, as it is pretty easy to do and will not hurt doing it again, but will have to be after work tomorrow. I will also try rotating the crankshaft back after I stroke is on #1 TDC to check total distance to timing mark travels before rotor begins to move. I hope I did the test wrong.
  8. Correction, the cam timing is retarded (intake close timing is delayed). Valves are still open at TDC. I don't hear slap or rattle form chain. Intuition is telling me this was done on purpose.
  9. Every cylinder same results, 40-50% leakage through intake. If I run crank till valves are closed, the air pressure runs to the engine to the next cylinder and reads 100% leakage. I've always thought my cam was not in time for a few years now. That is now confirmed. Why is it is the mystery. I suspect someone has been in there and done some engine work. Block and head are not stock looking color, valve cover has been replaced with an aluminum cover (not really a good one but it shows someone was dressing her up), odds and ends. Compression is pretty darn good for a 170xxx 4.2L being over stock specs. My hypothesis (not geometry) is a rebuild. Maybe the head was shaved too bump compression chasing a few HP? New cam profile timing chasing top end HP? I have no idea. Or maybe the chain just jumped.
  10. #4-50% leakage, #2-40% leakage, all through intake valve. Odd. Run up to #1 visually into cylinder as I rotated by hand and I could see no cylinder movement as I rotated crank. Timing mark is at 4* before TDC. This would make sense as I tried 4* and it backfires through the carb. So it appears that my valve train is not in time and advanced about 3-4*. Now, is that from chain slack and it jumped, or because someone has been in there and tried some "special" timing. I'm going to see what I can do for the rest of the cylinders.
  11. The adapter could have been missing. I hope this one will works. So I have an 1971 DJ5 that I acquired a while back. It was cheap, has lots of issues. Anyways, I thought that pulling the head from the DJ would be a good practice run to see what it will be like pulling the head of my CJ. The bolts are bolts, you turn turn turn them. But lifting that monster of a head off the deck, dam! That head is a beast! WD40 seems to loosen carbon reasonably. Add some elbow grease and brillo pads and it works wonders on removing carbon. So cleaning the carbon won't be too bad. Removing the head will be a chore. Installing the head, that will be a challenge without damaging the head, mating surface, the gasket, my fingers, back, or some other part of my body! A hoist would come in handy for this job.
  12. Looks like what my second order is but with different name. https://www.amazon.com/5573A-2-Gauge-Cylinder-Leakage-Tester/dp/B000OUX9PO/ref=sr_1_19?dchild=1&keywords=leak+down+tester&qid=1619479896&sr=8-19 We shall see.
  13. Harbor Freight was a bust. I tried O'Reily's, Autozone, and NAPA, same thing. I am really disappointed, yet not surprised at this point. Maybe part of the problem is the Jeep cylinder head? I have never paid attention and noticed any engine I worked on (Ford, Chevy, Dodge), but there is a 0.25 inch gap between the threads to top of head. Maybe my Jeep is the issue and not the tools. Whatever is going on, it is what it is, I will adjust. The good news. I received an email that my order has shipped! Hurray! Since discretion is the better part of valor, I will yield to caution and be patient for the kit to arrive. It will just be a little longer, if it even works, to see numbers. In the mean time, I will try a little Techron or similar product in the tank, and the old misting or small drizzle of water into TBI for a little steam cleaning in the mean time. Hoping that the next kit will work. Fingers crossed.
  14. Well, kit showed up but with no adapters and the hose will not fit into the cylinder. The threaded end is too short and it will not engage the spark plug threads. No adapters available. I cold spend my time trying to find/make and adapter, but may not work. Returned kit. I looked at others on the web and they all look the same, short threaded section. One appeared to have long enough threads, but will not ship until mid-May. I could spend top dollar for a professional kit. But all these options are beginning to the hit the extreme ends to me. Too cheap, too expensive, or too long of a wait. This brings me to a cross roads. I can go to Harbor Freight and see if their units have long enough threads to engage so I can start the diagnostic process now. Or just pull the head, clean and inspect, which is probably what I will end up doing anyways. My pressures are goodish. I am going to see if the HF kit threads are long enough to work. If not I will start pulling the head to be done with it and move on. The saga continues...
  15. In chassis was not considered except for a head pull to clean. Maybe if there was a fixable issue with one cylinder, but not likely. If she needs disassembly then she is being pulled. That kind of work is a pain I'm not likely to consider. First, I need to find a trust worthy machine shop to get an estimate for the machining cost on a rebuildable block/head. I've built a FE390 20 years ago. The total cost for machining and parts was about $1200 dollars then plus my time. But inflation, tools and current location will likely limit the ability to do work myself, or make it challenging at best. The cost to machine, rebuild parts, transportation to and from shop, and/or paying a shop to do the work will all be calculated. There is a tipping point between cost and convenience for everyone and we each must find our balancing point. Looking into crate motors, really doesn't exist for a 258 (that I have found). Not really interested in giving up my original motor anyways. What options I have found for the 258/4.2L are close to the same cost for a crate stroker and I must send then my engine for them to rebuild. The shipping will eat up any savings I could have saved from ordering a crate motor and might as well keep my local machine shop employed. However, that just makes ordering a crate stroker motor a financial smarter decision. There are several options for strokers: kits you put together, short blocks, long blocks, and turn key which is an option but is mucho dinero. Again, is is about finding that balance. To adapt a stroker and keep some of my parts, I will need a new exhaust manifold for the corresponding year of engine. the 258/4.2L exhaust manifold will not work. On a 87-90 and 91-95 block, from my research, my 4.2L aluminum intake manifold can work with slight modification to fit. However, I'm not interested in the modifying my intake. That action potentially could make the change back to 4.2L block irreversible. The availability of the 258/4.2L is not as common as they use to be and I want to keep integrity of the engine and parts to best I can. Clifford makes a carb intake for the 4.0L that I can use my TBI. Finding the balance. There is a lot to consider. I don't want to get too far ahead but I do have to think about my options. All decisions have merits and consequences, along with unintended outcomes not foreseen. No more philosophy. Still waiting for leakdown kit which is a bummer. I was hoping it would arrive today. My intuition tells my engine just needs a little hygiene work on the inside. I am enjoying the learning process and diagnosis procedures. There are so valuable in a disposable age.
  16. Less sleep deprived now. Leakdown kit it should be here tomorrow, but I imagine it will be Saturday before I can get some numbers. The budget, well I am always looking so save where I can but a full rebuild is in the budget if needed. However, a head removal and cleaning is the best I can do in my current situation. It is not permanent, but impactful. To pull apart the head is just not in the equation currently. It is what it is. However, if conditions of valves and head determine that a full head work is needed, I will be looking for for a machine shop for block and head work. I am not doing the top half now only to do the bottom half later which would require pulling the top half off I just did. Make no sense. So if that is the case, then I will be asking some different questions concerning the 4.0L head swap. But that is getting a head of the situation. I will review all the information you presented to me, along with me Jeep shop service manual. Until then, thank you. More to come Saturday.
  17. Point of correction from last message. I stated "hypotenuse". It should have been "hypothesis". My bad, but I am working on 30 min of sleep in the last 48 hours. Power nap coming. Wow, lots of good stuff here. I was not aware of the ping issues as a whole for the 4.2L. The worn out emissions components from the factory labored it horribly, hence the Howell TBI. The Mopar MPI was just too pricey. I currently have the stock distributor and went back to the Dura-Spark module. I could not find my CARB sticker for the MSD, so had to switch back for emisions testing. I'm not getting all that advance through mechanical, vacuum, or both. I know the dizzy has issues. I am running and have verified that ported vacuum is going into the dizzy-vacuum canister. As per timing at 8 degrees. Howell instructions state 6-8*. The engine for the most part around town likes the 8* for my overall DD. That would have to change for a mountain run. I will try 6* and see how that goes. I would love to put a D.U.I. HEI on her to simplify the engine compartment even more. Of somewhat concerning is if I try 4* I can get backfiring through the TBI. I think that is an indication that I have a little too much stretch in the timing chain and may have jumped a little. At 170,000 miles with issues, it is definitely time to replace before a catastrophic failure happens. Dang Moses, the more I dig into her.......She runs pretty good, smog emission numbers are very good! Low RPM is okay, not like it use to be after the nutter bypass and before Howell TBI. Mid power is okay, good enough to scoot down the Interstate. I will see what I can do with the leakdown test.
  18. Thanks for the great feedback Moses, I do appreciate it. To further your hypotenuse of carbon build up, I have to run 91 octane even on the flat land at 8* timing or she'll spark knock so those numbers may be pretty close. Driving up I-80 or Hwy-50 over the Sierra Nevadas is a slow drive. Running the leakdown will be an educational experience. I do believe it will reveal that the head needs to come off for cleaning and inspection. We shall see what it reveals. I do have a vacuum gauge (HF). It works, but it does not reset to zero. Easily replaced, they are not too expensive. I have checked the vacuum before. When I bought the Jeep, there was a dip in vacuum every now and then along with a ticking sound from the 5-6 cylinder area. I changed my oil, put some good ole Mystery Oil in, some Lucas Fuel treatment in the gas tank, and changed my oil every month for about 6-month, along with a little water down the carb (pre-TBI) to steam clean the cylinder. It was recommended to me and I was told it was safe as long as I use a small amount of water. This was a while ago. The ticking and vacuum drop has pretty much disappeared after , though the ticking has started once again. Oil pressure, well the gauge stopped working 2-month ago. Before it quit, warm idle was around 40psi +/-.
  19. I did the compression test again, this time with throttle open and original numbers had errors from that. Also, my HF gauge and the supplied adapters will not thread into head. I had to use the tapered rubber tube. I verified what will give me the correct angle to help insure a proper seal. New:1-155 / Old:1-160 New:2-157 / Old:2-135 New:3-165 / Old:3-150 New:4-150 / Old:4-140 New:5-180 / Old:5-125 New:6-165 / Old6-160 Assuming the gauge has a 5-10% error, numbers a pretty good, if not great, for a 170,000 mile 258 (sans #5). If the gauge numbers are correct, that is a little high for a Jeep with 170,000 miles. I will preform the leak down test when kit arrives. All in all, this is interesting stuff to me. I hope others can learn form this.
  20. Great advice Moses. Yeah, $400 was crazy. For a 90 min test, that is 😮! I did not have the throttle open and not sure how much that will impact the readings. No issues redoing the test as it is pretty easy. I have a 30-gal 200-psi compressor so good to go there. If I buy a tool, i subscribe to the philosophy Buy once-Cry once. I saw the HF on clearance for $25. I will leave that for those who have a tighter budget. I saw the OTC gauge and looks satisfactory for my shade tree work. I will rerun the compression test and report on the leak down when my gauge arrives. In the meantime I will be searching for a quality machine shop (not the previously mentions place).
  21. I was quoted $350-400 for leak-down test. Wow, that is $400 that can go to a rebuild. Does not make economical sense right now. So, I did my own compression test with a Harbor Freight (HF) compression test gauge I bought. Not sure if numbers are accurate (either the gauge or the tool working the gauge). 1-160psi 2-135psi 3-150psi 4-140psi 5-125psi 6-160psi #1 and #6 numbers are above the service manual listed specs for cylinder compression. Also, the cylinders next to the higher ones are lower. The service manual states 120-150 psi and no greater than 30psi between cylinders. I am outside of spec for both. Could I have a cylinder to cylinder compression leak? If so, then my head needs work (the jeep's head that is). No oil consumption only blow-by, no water in oil, no oil in water. I will be looking to see if HF or some other manufacturer makes a cheapo kit for leak-down testing. Or maybe I can make my own if it is not too prohibitive or costly. For the right price, it is worth investigating. Odds are I need to pull the head, so $400 to test for leak is $400 that will go for the cylinder head work. Or maybe a good time for a 4.0L head swap......that could be fun. More to come.
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